A special guest blogger to Quinntopia! As some of you may know, I had a Rivarossi 231 steam engine, but with some of the changes and directions of my hobby, I decided to sell it on eBay last summer. I was pleasantly surprised to hear from Terry in Delaware a few weeks ago who identified himself as the new owner and winning bidder of said eBay auction last summer! Terry and I started a dialog about these neat little Rivarossi locomotives and he proceeded to share with me the challenges and discoveries he has made with this locomotive since it has passed to his ownership. I was fascinated with his passion to restore this model (and somewhat chagrined to discover it was probably in worse shape than I even realized when I sold it) and his attention to detail in the process of restoring and describing the process. I was so impressed, that I asked Terry if he would be willing to share his ‘story’ on my blog, and he agreed! So here you have Part 1 of the unfolding drama that is the interesting journey this little Italian model of a French steam locomotive! Please feel free to post and ask Terry questions as well! – Jerry | Quinntopia
With apologies to The Italian Job and The French
Connection.
Subtitle: Locomotive Repair for an N Scale circa mid-1980s
Rivarossi French SNCF 231E 22 Class Chapelon 4-6-2 Nord Steam Engine and Tender
While this essay does not have anything to do with these two
classic movies, for some odd reason they came to mind when I made these
repairs. And when I am referring to The Italian Job, I mean the circa
1969 version with Michael Caine, Noel Coward, and Benny Hill amongst others. The
movie with the circa 1967 and 1968 Austin Mini Coopers. Well, that is another
story. Let’s just say that I am not young, and I also have a fondness for
British Cars.
Now - on to the real reason for writing this expose. Most of
us recall, perhaps with a gentle smile, the often quoted saying: “beauty is in
the eye of the beholder”. Well I think I have a story for you.
I must disclose that had one of my local train shops in
Delaware not been preparing a move in early 2014 this story might never have
happened. But for those train purists and aficionados, I just had to look in
the display case. You know, the locked glass one with many shelves loaded with the
older, unloved N scale trains. Where the ones that no one wanted reside, one
hidden under another. Glass shelves and cardboard boxes littered with all the
‘winners’ and ‘duds. The items where you have to ask for an attendant with a
key to unlock the mystery. That is how this all started.
There it sat in its original Rivarossi (RR, or “Rivvy” as I
like to say) polystyrene case, with nest, liner, and identification card. Complete….
And with the handwritten note on a little white paper sticker on the outer case
lid: “Static Display - Does not Run ”. Well, I should have turned and run the
other direction. Sadly, or perhaps poignantly, that is just not my nature.
Nope, I just can’t pass the odd ball or unusual item. That is how this all
started. The hook was in and set.
Anyway, that little ‘gem’ had a price of $40.00 for it. But
I managed to do even better negotiating with the clerk and owner. Remember that
moving sale. Well it moved into our basement.
That loco, in all its beauty, warts, uniqueness, and
brokenness turned out to be an N Scale circa mid 1970s Rivarossi French Steam
Locomotive 231E22 SNCF Class Chapelon 4-6-2 Nord brown color. The US item # (according
to the case is 4091), and the production date was 8-75 based on the
identification card. The Italian or EU Nord brown version is usually called 9181,
Locomotiva a Vapore. It is also sometimes called the Flèche d’Or. (The
numbering of these is a story in itself as far as I am concerned. I will save
that perhaps for another diatribe.)
For the nice price I obtained it I decided I was up for the
challenge. I got a good deal. Surely I could tackle this beast and get it to do
something. How short one’s memory can be. (Remember the dates of the movies I
like? And don’t forget that I am not young….. so it is easy to forget certain important
things.)
Many of us will recall the metal amalgamation (a nice word
for it that I can actually print for this public website) sometimes called
‘zamac’. You know, that flaky, silvery, metallic, off-colored sometimes putty
soft or something less than solid casting that was used to make many of the
chassis and frames for these vintage N scale locos? In the case of this model,
it is tender driven or pushed. The steam locomotive, while perhaps beautiful is
just a trophy pushed around by a tender. Not the best combination, but a little
odd or unique. So for those fans of the Pacific Light and Heavy 4-6-2 N scale,
we all recall that we should not look at the chassis under the shell crossly or
say mean things. It will turn to dust. And don’t dare drop that 4-6-2 on the
front snout. The shell will survive but that weak front nose – well. A nice
clean break point. Now you have two locomotives and spare parts to use or sell.
For those not familiar with this model here are pictures of a
few nice examples. This model came in a couple of different colors: Nord
(brown), Black, and Green (with matte black boiler front and baffles). They
really are exquisite looking visually, at least in my opinion, Kind of like an
early E type Jaguar convertible. Even when sitting still and not running, it is
quite a beautiful car. The following pictures are actually from a Rivarossi Memory‘IT’ (Italy) website with HO details for this locomotive class, but they show
the livery and details of them I believe I recall reading that for certain European train designations, the
“231” (as ½ of a 4-6-2) is their way of calling out the drive wheel
configuration.
The unusual aspect of this Italian made N scale French 231E Chapelon
with the tender pusher is that the frame and mechanics of the locomotive are
unique. In the case of this modelling the steam locomotive is ‘saved’ from the
‘zamac’ deterioration. That luxury is instead reserved for the tender. The
tender drive has the ‘zamac’ housing that contains the motor and drive gears.
And thus, it is the tender that has the crumbling, exploding, deteriorating,
metal amalgamation that can turn to dust or a pile of Fool’s gold at the drop
of a hat. (I will delve more into that in a later writing.)
But I was determined and set out to work on this one. And as
I studied the tender carefully, it was apparent that the all-familiar ‘metal’
cracks, hairlines, expansions, crumbling were present. But I was kind of lucky.
It had not gotten to the point that it exploded the thin tender polystyrene
shell or case. No this tender shell got lucky. Somehow it had escaped. But not
the softer styrene truck carriages and motor drive gear support housings. They
were getting pushed out of alignment and breaking too. Yep, she was in bad
shape.
With time it became apparent that ‘static display’ was
correct. No, I was not the lucky one. So I set on a quest to find a couple (how
about one!) of these that was in good shape. Running and not going all to metal
dust. It would be the holy grail of N scale Italian made French 231E
locomotives. There must be one somewhere! Right? Surely this would be a short
quest.
Over the next year or so I explored and found a few of the
Rivarossi French SNCF in N scale. Some decent, some not. Interestingly the best
one thus far is the version in black livery. It is exquisite and runs quite
well. It came from a fellow train enthusiast in Germany in an original plastic
soft shell case. But like those British cars, this pristine example is really a
trailer queen. You know, not used, nor driven, instead only to be looked at. To
take up space in a garage or basement. (As I write this, I jokingly wonder:
maybe that soft shell outer case was to accommodate the expanding tender in
case the metal started to swell, at least it would not crack the polystyrene outer
jewel case.)
One of my recommendations if you have one of these models:
if the tender has not exploded or crumbled yet, and the tender shell is in good
shape - buy a spare jewel case. Carefully remove the tender motor housing from
beneath the tender shell. Store them separately. (My other belief, not at all
substantiated, is that some of the early lubricants, or cutting fluids if used
as a lube, are based not just on petroleum hydrocarbon cuts, but may also be
vegetable or fatty acid or ester-based lubricants. If true, I suspect those can
deteriorate with heat, age, and oxidation, possibly even forming other chemical
species that can further deteriorate the metal. Just a theory and no proof.) So
the inherent caution, be sure to use good lubricants. And as one of my friends
likes to say, the original grease turns to ‘peanut butter’. And that sure is
true. I suspect that all the ‘light end’ or low boiling petroleum constituents
evaporate leaving the ‘sludge’. And that poor crumbling locomotive or tender
has to crawl through all that with only 12 volts, and on a dirty track. Perhaps
that is not a good combination.
And all that brought me to the version that I write about
today. This particular SNCF 231 (4-6-2) was offered. And like many it had its
shortcomings. But it ran. Visually it was another story. No this one would not
be going to the prom. Someone had gotten carried away with superglue and in a
not so good way. Anyway, at least it did not say static display. And its early
bid prices were not that unreasonable for a runner. Time cured some of that,
and I was hooked again.
So I conquered it and it was mine.
This one moved into our basement to sit along with the others. And after about
6 months I decided to look at it closely. Here is a picture of it as received.
It is a circa 1980s vintage, 10/1980 production according to the case
identification card.
This winter I set about taking this one apart. I gained a
little confidence from a friend near Pittsburgh, Pennsylvania who has been my
go-to on these things. We met recently and he has been a remarkable resource
and guide. He suggested I get a lit loop which I did. It is only 3 ½ inch LED
lit but it works nicely. He also has instilled in me wisdom and confidence with
sound advice on working with these things. I think he could repair and get
these N scale locos running with both hands tied behind his back and
blindfolded. Graciously he did look at one of the other French SNCF 4-6-2 locomotives
I have cleaning, adjusting, and lubricating it and got it running like a Swiss
watch. It works nicely, and his advice once he returned it to me was “sell it”!
I love a good chuckle or laugh.
So I grabbed my X-Acto knives, jeweler screwdrivers, cigar and
candy boxes and started at it. Back to that surgeon…. For some odd reason, the
center boiler shell top screw was so tight I needed a ½ inch drive socket to
get it loose. (Just kidding – but it was close.) And just when I thought I was
clear, it became apparent that the right side boiler tube down through into the
valve piston box (or whatever it is called) had been glued. More CA and lots of
it. So I had to carefully cut through the pin that protrudes down into the
piston box. That was difficult. And unfortunately there was no way not to carve
it up a little bit. Thankfully only the right side was glued. Not the left.
Whewwwwww it had escaped that doomed fate. Note this
picture shows in the background the bulb still attached to the cut headlamp
bulb support bracket.
So I got the boiler shell up off of the apron or lower
chassis.
And then the strange brew of the rewired headlight became clear. To make matters worse it was soldered and barely fit within the housing. Silicone had been used. The headlight bulb mount post had been cut about halfway up. About the only good news was the front smokebox boiler cover was still there. It had been installed in backwards. And it had a hole drilled in it, embedded brass tubing, and a light bulb sticking out through it. At least I would not need to fashion a new one. Or so I hoped. Here are more pictures of some of the progress.
And then the strange brew of the rewired headlight became clear. To make matters worse it was soldered and barely fit within the housing. Silicone had been used. The headlight bulb mount post had been cut about halfway up. About the only good news was the front smokebox boiler cover was still there. It had been installed in backwards. And it had a hole drilled in it, embedded brass tubing, and a light bulb sticking out through it. At least I would not need to fashion a new one. Or so I hoped. Here are more pictures of some of the progress.
A brief digression for a moment. Here is some advice that I
have received and I pass along. I also learned this working on British cars.
The early to mid-1970 chrome bumper MGB and MGB GT are two of my favorites. Remove
pieces carefully, photograph, document, and understand their removal and
installation carefully. Do not throw anything out. I repeat - don’t throw
anything out. Ever. (Even after you have completed the job. You may need that
spare someday.) And better yet, have a spare for comparison. You know, what
good is one MGB? No have two. One you can disassemble and the other as a
reference point. I am only half joking. I still own two MGBs. Of course you may
need your wife’s buy-in on this point.
Back to the Rivvy, careful work with a fine point X-Acto
knife and I was able to free the boiler shell from the CA glacier. I also got
the air tanks free and cleaned them. The biggest decision now is whether to
attempt to repaint them and the upper boiler shell, or just consider it the
results of a bad weathering job. I think less may be more. I invested in a
couple sets of wire gauge drill bits. And I used them to clean the holes for
the air tanks. The latter two pictures still show
the front smokebox cover inverted and inserted into the front of the boiler.
They are actually from an earlier portion of this rebuild.
Next I set to tackling the chassis. I was not sure how much
time I wanted to invest in repairing it if it would not move smoothly. After
careful realignment (and extra bending) of the side rods and valve gear, and
spreading the valve gear vertical alignments it began to move better. I then
removed the front and rear trucks and cleaned and straightened the axle wiper blades.
(Power from the right rail is carried through the conventional ‘drive’ right
side wheels ( the ‘-6-‘ in this case) which is carried up through the chassis
apron via a front metal contact plate and to the headlight mounting post base.
The other (left) rail current is carried through the left drive wheels and tender
draw bar needle and pin post to the rear of the loco chassis and a rear metal
contact plate beneath the boiler. Sort of an ‘iffy’ arrangement but once
repaired it has worked. And how they got all of this crammed into the small
space of these N scale locomotives is a marvel unto itself.
Weight in the locomotive shell comes from a steel rod
secured inside the shell. The bottom has a screwed spring clip that contacts
the chassis rear metal contact plate. From the top front of the rod protrudes a
soft metal spring that contacts the center post of the lightbulb when it is
placed in its mount and the boiler shell carefully lowered over the chassis
apron and its workings. The other line to the bulb comes from the bulb support
post that is riveted to the chassis front metal contact plate. I decided early
not to drill rivets and attempt to replace them. The geometry would call for
very fine rivets and long nose rivet gun and points to get that done. And I
feared it would be fatal to drill the rivets.
My next challenge was to rebuild or remake the headlight
bulb support mount. Upon getting it apart it was apparent that the CA surgeon
owned a Dremel or perhaps a large chop saw or grinding snips. Now a dilemma.
How do I rebuild that? I had already determined I could remake the mount. But
how to attach it? I suspected that soldering could melt the chassis apron if
not done carefully. And if I decided to drape the remaining carcass with wet
cloth while soldering that would probably pull too much heat from the
attachment point, rendering a solder attempt futile. Maybe I could use a
metallic epoxy and solder thin wires to connect the points. That was what I
decided to do. First I would make the replacement piece. Then solder thin wires
to it. Attach the new post support to the remaining base with epoxy then solder
the wires to it. For the wire I used very thin gauge stranded wire intended for
illuminating N scale passenger cars with LED lights. So I set out to make the missing
headlight support mount top post.
This was much more fun that I thought. Because I got to head
out to one of our local True Value hardware stores. I knew deep in my mind they
would have what I needed. So I set out with my youngest daughter after her
swimming lessons for the True Value. (P.S.: I have learned the knack of
convincing my daughters that they will find something (that I like) really
interesting. This technique has worked well, and so they frequently enjoy
watching ‘their shows’ which in some cases are actually ‘my shows’. Dual
Survival, Pawn Stars, Counting Cars, Fast and Loud, Swamp
People, and Alaskan Bush People are good examples. This is particularly
useful when I would like to watch my own TV in the house. I don’t know how long
this trick will work but I am enjoying while it lasts.)
Sure enough True Value had a nice assortment of various thin
gauge metal strips, rods, and threaded rod. So I bought a strip of ¾ inch wide
0.016 inch brass and another of 0.018 inch steel ½ inch wide. And a few of the
smallest brass screws and washers just in case my solder and epoxy effort
headed south.
I took apart the companion locomotive, a good shape green
version that I obtained from a train enthusiast in Italy. I made some
measurements and then began to prepare the brass (The
reference factory NOS locomotive assembly is to the right in the picture.)
Things
did not turn out too bad as evidenced by the accompanying photos.
After several scribes with a
knife or awl, cuts with a hacksaw, snips with sharp tin snips, drilling through
the brass clamped to hardwood, filing, bends in a vise, more nips with a sharp
pair of nips it was getting close to finished. Fitting it within the narrow
confines of the boiler shell and able to still stay forward of the steel rod
(the other rail’s current) was a challenge. I also decided to place a few
pieces of clear thin tape on the front of the steel weight rod just in case the
tolerances are tight. This part of the rebuild took many fits, adjustments,
refits, filing, clipping, etc.
Then I again pondered the best means to attach it to the
post. I initially planned small brass screws and washers. I even drilled a few
(not quite centered) holes in the new bracket for the screws. But I again
noticed the tolerances were tight and that might not work. (But I also drilled
those holes knowing that if need be they could be solder channels.) I finally returned
to settling on using wires and epoxy. My concerns were the heat needed to get a
good solder joint could wreak havoc on the plastic apron or lower chassis
structure, as well as the small clear polystyrene headlight ‘tunnel’.
This model has an interesting light tunnel to transmit the
light bulb’s illumination to the two small front headlamps that reside on the
front apron. (Perhaps this caused an earlier owner to deviate to a new bulb
configuration? I do not know, but I hoped to return it to its original
configuration.) The original design is a small polystyrene piece of plastic
that sits below the bulb, fits forward of that area and resides above a metal
lower panel on the chassis bottom to hide the light. It travels further forward
to the two narrow light channels. In this photo the
rearmost portion of this polystyrene light tunnel sits just forward of the base
of the headlight bulb vertical support post. This is sort of like the earliest
days of fiber optics. And actually it works fairly well. But, maybe the cost or
difficulty in finding a new bulb caused a change of course for a prior owner.
The final configuration for the replacement bracket piece is lower left center
just forward of the loco chassis.
I was still convinced that too much heat and flux could warp
and melt the entire jumble. So I set about attaching the very narrow stranded
wire. I first thought I would place the wires at the upper ‘head’ of the new
bracket piece aside the bulb, but concluded it was too narrow in the boiler
shell. I decided to place the strands on the bottom reverse side of the new
bracket.
So I set about cleaning, sanding, and using 0000 steel wool
to clean and roughen the pieces to attach the wires and epoxy. I had also
determined that I could place toothpicks below the remaining bulb support base
and that would raise it just enough to not touch the plastic headlight tunnel
piece. And I then began soldering the wires to the bracket. And as I did that I
convinced myself that soldering would be best. Good old impulses. If I could just
do it quick, hot, and neatly. So I used an alligator clip to hold the new bracket
support piece to the remaining post. I placed toothpicks to raise the metal
bracket off of the light tunnel. And pondered a little more. Now what project
is fun without being dangerous or unhealthy?
My last challenge was having only two hands. And I was not
going to go and buy a positioning vice. Nope, not me. So I got started and
quickly found my limitations. And so, with hot soldering iron, smoking flux –
what else – yes I pulled a three foot strand of my 60/40 rosin core solder and
clipped it. One end in the mouth between teeth, and worked quickly. I was able
to get a decent joint. And I then attached the other ends of the stranded wire
for good measure. It turned out fairly well. And the plastic light tunnel was
only slightly melted or altered by the dripping flux. Ok, so
I am not perfect. A perfectionist yes, just not perfect. Darn it.
To be continued in Part 2...